So this Saturday morning I took the plunge and dove into the manifold replacement project.
In preparation for this work I nosed my truck into the garage and had the front end suspended on jack stands.
I then removed the negative terminal of the battery and removed the front wheels and fender liners. The only other item I had to remove for access was the y-pipe and disconnecting the 4 connections for the o2 sensors.
With all of that out of the way, removal of the stock manifolds was very easy with air tools.
If you were to perform a manifold replacement only, I can see how this would be a 4 hour job. Swapping out headers added another factor of pain and suffering.
Problem #1: Fasteners
When my AFE headers shipped, I only received 10 grade 8 bolts out of 16. Originally this wasn’t a big concern because I planned to upgrade with ARP fasteners. When I opened my ARP fasteners and tried installing them on the headers before installation I found out that 5 of them would not fit in the holes due to interference with the tubes. MAJOR disappointment. So now I had to use the grade 8 hardware supplies by AFE. I ran down to my local hardware store and of course they were out of the bolts that I needed to make up the shortage of bolts not provided by AFE so this meant more time on the road looking for bolts.
The second fastener related issue I found was that on two of the holes at the back side of the headers, the bolts provided by AFE don’t fit. Nowhere in the instructions is this mentioned.
So I stopped, and amazingly refrained from cursing and thought about my options. One, notch the holes and use the ARP bolts, or two, use a combination of grade 8 bolts and run back to the store and buy some studs and nuts. I opted for #2.
As I mentioned before, 12pt bolts are wonderful in tight conditions, and as I installed the grade 8 6pt bolts I was imagining how nice it would have been to have the 12pt heads to work with. Installing the headers and following the torqueing sequence is a pain, more so on the driver’s side. This is all hand work, with probably 40% use of sockets(no air) and the rest being ratcheting box-end wrenches. And therein lies a problem. You are to torque these bolts to 18ft-lb but getting a torque wrench on most of these bolts is near impossible. With this in mind, it’s a matter of feel, comparing the spec-torqued bolts with those torqued by hand.
In all, with weekend distractions, hours of driving to and from stores looking for fasteners, this took about 12 hours, wheels up to wheels down. Without fastener issues I’d say 8 hours would be a realistic time frame to set aside for this project.
I’ve got a very slight leak that I need to fix at the collector and y-pipe connection but its minor and goes away 20 seconds after starting the engine. I’ll make this repair once I drive the truck for a week and recheck all bolts for torque again.
Driving impressions are... I can’t honestly tell a difference beside the fact that the truck doesn’t have a bad exhaust leak from the factory manifolds any longer. I saw more seat-of-the-pants change using my pedal commander than I did these headers. I’ll monitor fuel use over the next two weeks to see if there are any gains there. If I ever pair my headers with some aftermarket exhaust, perhaps it will sound nice, but at this point I’m not interested in dropping any more coin into my truck for some time.
Would I recommend AFE headers? I can’t say that I could without reservation. I’d like to hold a set of JBA’s to compare the quality but for the same price you can get them factory ceramic coated. I’m not sure if JBA’s have the bolt clearance issues either. That fastener debacle was pretty frustrating and cost me many hours of my life.
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